Hi-Lo and Black Bear . . .

Today was an easy one with lunch at Gator’s and then an HEB stop for some things.

And that was about it.

So I thought I’d do a 2 Day blog repost from May 2017, our last year on the road. We were on our way from Weed, CA to Bend, OR, with an on-the-road Allison transmission repair in the middle, for a little extra fun.

May 2, 2017

May You Live In Interesting Times . . .

There’s a reason this is considered a Chinese curse, though apocryphal in its origins.

And today was very ‘interesting’, though it started out nice.

First up though, I’ve fixed the photo problem on yesterday’s blog, so you can scroll down and see all the pretty pictures. I don’t know what happened, but I’m pretty sure it had something to do the WordPress database problem I had last night.

Wanting to get to bed a little early, I had the blog ready to go about 11pm, but it wouldn’t . . .  go, that is.When I tried to upload it, it kept telling me it couldn’t write to the database. Now weird things happen sometime, maybe Godaddy updating the WordPress software at the same time, etc. But after waiting about 30 minutes with no luck, I put a call in to Godaddy.

Talking to the support guy, and trying some things, I found I couldn’t make ANY changes to the blog at all. I could read old posts just fine, I just couldn’t write new files to it.

The support guy suggested I restore from backups back to yesterday’s blog, basically just overwriting the entire blog, over 3000 posts,and1000’s of photos and comments..

So with a loud GULP I hit the Restore button.

The progress immediately jumped to 70% and then stayed there, never moving. So after about 30 more minutes, I went to bed.

When I got up at 6:30 I found the restore had finished and the blog was still functional, so I click the Publish button and away it went. And a minute or so later it was done.

BUT . . .

being in a hurry I neglected to look over the new blog post, so I didn’t notice the photo problem. That became apparent when I started getting emails while we were at breakfast, but I had already shut down the computer at the rig, so it would have to wait.

Now back to this morning.

We were up at 6:30am, got everything pretty much ready to roll, and then were out the door about 7:30, heading to the Hi-Lo Café a couple of miles away in downtown Weed.

The Hi-Lo Café, opened in 1951, was the pattern for the Black Bear Diner. The first one was down the road in Mt. Shasta City  and started by the original owner’s daughter and her husband. Then when they got divorced, she kept the Hi-Lo and he got the Black Bear Diner. Which has grown to over 100 locations since then.

But still only one HI-Lo. And last year the 3rd generation of the family took over.

Jan and I pretty much had the same thing for breakfast. This is my version, a Bacon Belgian Waffle, two strips of bacon, and two eggs over medium.

Hi-Lo Bacon Waffle

Jan’s had a plain waffle, two strips of bacon, and eggs hard scrambled. Both delicious.

Heading home I got a couple of good shots of a lenticular cloud over Mt. Shasta.

Mt Shasta Lenticular Clouds 1

Mt Shasta Lenticular Clouds 2

In the second one, the clouds are rolling down the sides of the mountain like water over a dam. Stunning.

But Mt. Shasta is famous for its clouds. Here’s a couple from the Internet.

Mt Shasta Lenticular Clouds 3

Mt Shasta Lenticular Clouds 4

Just WOW!

Getting back the park I finished getting us ready to go. As you can tell I had pulled into the site backwards so we could see Mt. Shasta out the windshield.

Friendly RV Site

Due to our rig’s first owner ordering the ‘extra long power cord’ this is never a problem for us.

We were out of the park by 9:15 and heading for the Flying J a few hundred yards away. Across the road we could see the burned out remains of Silvas BBQ.

Weed Silvas BBQ Burned Out

We’ve eaten here several times and it was always good, so it’s a shame it’s not around anymore. They had a grease fire in a vent hood back in Nov. and that was it.

We were dieseled up, hooked up, and pulling out of the Flying J by 9:45, a little ahead of schedule for a change. But that didn’t last long.

As we started to turn on the I-5 entrance feeder, I noticed the rig was kind of lugging, not accelerating like it should. It was quickly evident that problem was that the transmission was stuck in 1st gear and wouldn’t upshift to 2nd. Then I happened to move my head a bit and saw a Check Trans light on the panel. I didn’t see it at first because it was blocked by the steering wheel.

No other alarms, no Check Engine light, no nothing. Just the Check Trans light. It was obvious that I was stuck in the ‘infamous’ Limp Mode.

So I tried the simplest thing first. I shut the engine off, let it set for a few minutes, and then started back up.

OK, no warming light. That’s good.

But as soon as I was moving a few miles per hour, the light came back on.

Bummer!

Jan however, said some other words.

So next I checked the transmission fluid. It was at the lower part of the OK range, but I added a little Transynd to be sure.

And again, no luck. Still stuck.

I did use my Silverleaf Computer Display to check for any fault codes, but nothing showed up.

So now I was on the phone to Spartan, my chassis manufacturer, to see what they might have to contribute. But not a lot, but they send me on to Allison Tech Support.

Now I have known for a while that my rig’s Allison transmission is kind of an oddball. I think it kind of straddles a model revision, or something. For example, according to my transmission’s serial number, I should be able to check the transmission’s fluid level from the console, but I can’t.

I’ve had several techs tell me I must not be doing it right, and proceed to show me how. But apparently they weren’t doing it right either.

The Allison tech told me to check for transmission fault codes by turning the key on, and then pressing the upshift/downshift buttons together, twice.

And I got nothing. So I turned the key off and back on, and then did it again.

Again nothing. But I did notice that something flashed in between the first and second presses. So I turned the key off and on, and pressed just once. And now I had the code display.

But no error codes were showing.

As we were talking and checking some other stuff, he had me crank the engine up, and for some reason I decided to try the code thing again.

And this time I had an error code, a 2-5-1-1.

So between the number of presses needed and the fact that the engine has to be running to read codes, are just two more weird things about my transmission.

The tech told me that the code meant that the rig was getting no output speed info from the Output Speed Sensor. And I was VERY glad to hear this, because a bad sensor was something I could possibly replace or fix myself.

The tech was kind of surprised I wanted to crawl under the rig and work on this myself.  He doesn’t know me very well, do he?

He suggested I check the sensor physically to see if it was still connected and didn’t look damaged from road debris, etc. So under the rig I went with my work pads.

And this is what I found.

Allison Speed Sensor Connector 1

It looked OK, but I wanted to pull it apart and clean it, in case it was just a bad connection. So I sprayed the area with Awesome and wiped it down, and then unsnapped the connector.

Allison Speed Sensor Connector 2

The wires looked good, so I sprayed both the socket and the plug with Strike Hold, let it sit for a few minutes, and then put it back together.

Now I was really confident I had fixed the problem. I mean Strike Hold will fix anything and everything, right? So I rolled out from under the rig, eager to give it a try.

Since I was working on the road side of the coach I set my step ladder along the side of the road to deter any close shaves. They might not have a problem running over me, but they probably don’t want to scratch their paint by hitting a metal ladder.

And yeah, I’ve got some cones somewhere, but they just run over those, too. I mean, look at all the dead cones you see, the life crushed out of them, their faded orange carcasses littering the highway.

But back inside and moving out, I still had the problem. So Plan B. We’ll limp along the shoulder until we get to the next exit, for downtown Weed, and then park in a large lot that I had seen, and then I’d regroup. And that’s what we did.

And along the way I noticed something new. I had no speed information on either my dashboard speedometer or my Silverleaf. And I had no odometer readings either.

So getting parked I was back on the phone with Spartan. I called them because they know both systems. Allison knows the transmissions, Cummins knows the engines, but Spartan knows both, or at least how they interface. And I wanted to know if the dashboard speedometer got its data from that the transmission sensor.

And yes it did.

Now I was on the phone to the nearest Allison shop, which was down in Redding 65 miles south. And yes, they did have the part in stock for $85 plus tax. So after unhitching, and parking the rig in the far corner, we were off for Redding..

I figured that replacing this sensor was my last shot at avoiding a 65 mile tow and a very large repair bill. If it’s like most of these sensors, you just unplug the wire, remove the bolt, pull out the sensor, stick the new one in, then bolt, then wire. Easy Peesy.

The trip down to Redding only took a little over an hour because it’s just that . . .down. Just about the entire way. And a lot of fun curves that make Jan hiss.

Getting to the Allison parts counter, I had the same oddball problem again. The sensor that the computer said I needed, did not look like mine. That one had the plug sticking straight out, but mine is at a 90° angle.

Allison Speed Sensor 29543432

But they finally found the right one, and $91 later we were on the way back to Weed. Getting there about 4pm I called the Bend TT to let them know we wouldn’t be coming in today and I’d let them know about tomorrow.

The above-mentioned Hi-Lo Diner, which was only about a block away, also has a motel and RV park attached, I figured I’d putt-putt down the hill and we’d spend the night there and I’d replace the sensor there. So after getting a site, off I went with Jan following in the truck.

And before I got out of the large lot, I noticed something. I had speed info on both the dash and the Silverleaf. Could it be?

And yes, out on the street, the rig upshifted smoothly  to second, with no lights or other problems. I made the 1/2 mile journey to the park with no problems, even hitting a large pothole that I held my breath, thinking the problem might return. But it was all good.

So did Strike Hold just take its time to fix the problem?

Did gremlins figure that they’d had their fun at my expense?

Or Did fate just want me to waste $91?

And Now The Rest Of The Story.

May 3, 2017

Traveling on the Al-Can Highway . . . In Oregon

We were up at 7am, later than usual, since we didn’t have much to do to get on the road. In fact we didn’t even put out the satellite dish last night, but just listened to music on our Amazon Echo.

We had a nice site that I just treated as pull-in, easy due to how the power pedestals were configured.

Hi-Lo RV Site

Of course we had to have breakfast at the Hi-Lo Café once again, especially since it was right up the hill and we had the free tokens for coffee that we got when we checked in the RV park.

Since we both had leftovers from yesterday’s breakfast, we decided to go smaller this time.

So rather than the full waffle, we got their 1/2 waffle combos.

Hi-Lo 2nd Breakfast

Still delicious, just less of it. And no leftovers to try and fit in the fridge.

The first time we ate at the Hi-Lo in 2011, I noticed this logo on their coffee cups.

Hi-Lo Al-Can Hwy Mug

When I ask about it, they said it’s true. US97 begins in Weed and runs all the way up to the Canadian border where it becomes PH97. Then PH97 runs up to Dawson Creek where it picks up the Al-Can name. The Al-Can stays US97 until it becomes PH1 as it passes from British Columbia into the Yukon Territory right before Watson Lake..

So I think they make a pretty good case.

Back at the rig we were pulling out of the park by 9:15, Jan following me in the truck so we could hook up on a side street.

Driving through the park, everything was fine and I had speedometer readings on both the dashboard and the Silverleaf.

That is, until I hit a bump. Then the problem was back.

Bummer!

Jan, as before, said other things.

So I just circled back around through town and right back into our space at the park. Looks like I was going to have to change out the sensor after all.

After I got shore power hooked up and the slide out, I walked up the hill to the office and told her that we were either back for an hour or so, or a day or so until we could get towed to Redding. She said no problem.

I did see this really nice 1949 Oldsmobile coupe parked by the office.

Hi-Lo 1949 Oldsmobile 1

Hi-Lo 1949 Oldsmobile 2

The emblem on the rear deck indicates that the original buyer paid the almost $200 extra cost for the optional HydraMatic automatic transmission,more than10% of the vehicle’s cost.

To make it a little easier to work under the rig I raised it up on the rear levelers as high as I could, giving me plenty of room. Next up I put a call into Jay, the Allison Tech Support guy, to ask him a question.

“When I pull this sensor out, am I going to have 150° Transynd pouring out on my  head?”

He said, “Good question. I don’t know. Let me check.”  And when he came back, he said, “No problem. It’s dry in there.”

Glad to know that I don’t have to worry about that.

Gathering all my needed tools, I was under the rig at 10:10 and done at 10:45.

Allison Speed Sensor Connector 1

The only slowdown was that I had to come out from under the rig to get my 18” cheater pipe from the truck to break the bolt loose.

Allison Speed Sensor Replacement 1

Pulling the old one out, I smeared a little oil from the O-ring on the old one to the new one, stuck it in, and then tighten the bolt back in place.

Allison Speed Sensor Replacement 2

So now for the big test. Either on to Bend, OR, or towed down to Redding, CA in disgrace.

After I got cleaned up, we were pulling out of the park by 11:30 with Jan again following me in the truck. I told her that if it was working, I was going to make several loops (about 1/2 mile each) around the town. If the problem returned I would just pull back into the RV park.

Otherwise I would go round and round a few times until I was satisfied, and then pull back into the large parking lot where we were parked yesterday when we drove the truck to Redding for the part. Then we would hitch up there and get on US97 for Bend.

And even though I was deliberately hitting bumps, the problem never returned. And it never returned during our 4 hour trip up to Bend, 195 miles north. Smooth as silk.

We got in to the Bend/Sunriver Thousand Trails about 3:30, parked the rig in the big lot, and drove the truck around looking for a site. We found a nice one with 50 amp and water, and what I though was a good satellite shot. But no luck on that front so far.

Bend-Sunriver TT Site D24

The last time we were here in 2013 all these front sites had sewer hookups, but no longer. The caps are sealed at the sites, and the literature says several times that there are no sewer sites available. Guess they must have had problems with their septic system.

Wrapping up, I found it really funny that all of the techs I talked during this recent unpleasantness were amazed that I was actually working on this problem without hooking it up to a diagnostic computer first.

“How will you know what’s really wrong with it?”

As I said yesterday, I was very, very happy to hear it was a sensor problem. Sensor problems are easy. 95% of the time it’s one of two things – bad connector/wiring or a bad sensor. That’s it.

And I always play the odds.

In addition, I really wanted to keep the rig out of the shop. The one time our rig was in the shop was in 2012 when we were coming into Los Cruces, NM and the engine just quit running.

Towed into a Rush Truck Center, I was already down $500 just in diagnostic costs by the time they found the actual problem. That turned out to be a sensor on the fuel line feeding into the fuel injection system. Another sensor.

Then it was another $200 to actually fix the problem. But in the meantime they’re finding a lot of other stuff that “really needs to taken care of.” And some of it I did do.

But if I had done everything they suggested it would have been a little over 7 grand. As it was, my bill was almost $3000.00.

Hopefully tomorrow will be a little less hectic.


Thought For The Day:


For Those Days When Your Tin-Foil Hat Just Isn’t Gonna Cut It!

Aluminum Man

  

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